Alright, it made it......now to get it out of the box and torn down this weekend so I can get the parts sent off to the machine shop on Monday.
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Project #2 is supposed to arrive tomorrow or Sat morning.....more on that when it gets here.
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Minidave Well-Known MemberLifetime Supporter
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Crashton Club Coordinator
I'm sure most everyone has a machine shop screw up story. There are a couple in my past. They taught me a couple of expensive lessons. After that I double check & then triple check everything that comes back from the machine shop. Being an old fart now the likelihood of me needing to use a machine shop is quite low.
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Minidave Well-Known MemberLifetime Supporter
I don't think the gas was the problem, I think he just mis-timed it and didn't realize the sound he was hearing was not a rattle but detonation. I'll get it running in the test bed and get the initial timing set, but the best way would be to put it on a dyno and set it there. He's running an electronic distributor that has a bunch of built in advance curves, we'll pick one that's not quite so aggressive.
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Minidave Well-Known MemberLifetime Supporter
Some more progress on this motor.
I installed the trick adjustable, belt driven cam drive kit and spent this afternoon getting the timing set right - 106* ATDC intake valve fully open. It took a while to get the set up right, then it's super easy to adjust the cam timing.
With that set I buttoned it up.
Next I'll go ahead and install the other pistons and torque everything up.
I also was lucky to find a couple gaskets for the center oil pickup in my spares stash. I don't think I'll be able to install the pick up unless I take the layshaft out first - with the screen on the end it's too long to bend around and fit in the opening with the layshaft installed.
With these things done the rest of the build will go much more quickly.....the head is done and ready to go on. with any luck by next weekend it will be headed back to Atlanta.-
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Minidave Well-Known MemberLifetime Supporter
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Minidave Well-Known MemberLifetime Supporter
All the other pistons are fine, I don't know about the spark knock, but it def could be and he just didn't understand that's the noise it was making. I think that's unlikely as he's a "car guy"......but it could be. The pattern is what's bothering me - seems like it would be worn all across or the bearings would be pounded flat.....
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Crashton Club Coordinator
Let me know how it goes when you get that new heim joint.-
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old81 Club CoordinatorLifetime Supporter
- May 4, 2009
- 1,542
- Used to work making computers run fast!
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Really make it all lookso simple and easy, last time I had a Sprite head apart was in 1967 and I had help from a great AF Master Sgt who ran the base hobby/machine and auto shop at SAC. Ah the days of being young and a bit ignorant of what my challeges should be.
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Nice work. Wish I had the space.
Don-
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Crashton Club Coordinator
Gotta love David Visard's A series bible.
Your head work has given me a flashback to porting the head on my Fire Arrow engine. There was zero info about how much to remove or where. No interweb forums either, just a newb with a die grinder. I managed to do it without grinding into the water jackets. My air compressor hated me & I hated it.
You do excellent work Dave. Bet you could do your own knee replacement.-
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Minidave Well-Known MemberLifetime Supporter
I did the same on a Fiat 124 head in 69, in conjunction with a Judson supercharger it really opened up the high RPM power, and I didn't really lose any low end.
Then my buddy overhauled the transmission - it was scrunching going into 2nd - and when he got done the 5 speed was now a 4 speed! somehow he's lost 5th gear - no idea how he did that! Kids!
I laughed at your idea of me doing my own knee!-
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Minidave Well-Known MemberLifetime Supporter
Fired right up, but before I could get the timing light on it or anything it died - I think my fuel pump crapped out - it was the old one off of Buzz, and the reason I replaced it off Buzz was it would quit on me - used to be I could get it going again by tapping on it, but no go this time.
(15) VID 20201209 141245 - YouTube-
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